L-1011 Accidents and Incidents


This is a brief description of the accidents and incidents that the Lockheed L-1011 has been involved in. There are also some links to more info that can be found on the internet. Read and learn.

December 29, 1972.

Everglades, Florida, USA.

Eastern Airlines N310EA.

L-1011-1 (serial no 1011).

Eastern Airlines flight 401 departed New York for a night flight to Miami. On approach to Miami the crew did not get a green "down and locked" light for the nosegear. They aborted the landing and climbed back to 2000 ft. The Flight Engineer climbed down into the Forward Electronic Service Compartment (FESC) to visually check the nosegear via a porthole while the rest of the cockpit crew also tried to solve the problem up in the cockpit. Noone noticed that the aircraft started a gentle descend which did not stop until the aircraft crashed. Of the 176 total onboard 99 died.

Accident description (ASN). Cockpit Voice Recorder transcript.


April 19, 1974.

Boston, USA.

Trans World Airlines (TWA) N31007

L-1011-1 (serial no 1026).

The aircraft was on ground when a fire broke out with major damage to the rear fuselage as the result. It was never repaired.

Accident description (ASN).


August 19, 1980.

Riyadh, Saudi Arabia.

Saudi Arabian Airlines, HZ-AHK.

L-1011-200 (serial no 1169).

The flight, originating in Karachi, made an intermediate stop in Riyadh and then departed for Jeddah. 7 minutes after takeoff, aural and visual warnings indicated smoke in the aft cargo compartment. The crew initiated a return to Riyadh from FL220. During the descend smoke was noted in the aft passenger cabin, the number #2 engine throttle was stuck and passengers (panicking) were fighting aft of the number 2 doors.

During final approach the #2 engine was shut down and the Captain told the cabin crew not to evacuate. The aircraft landed at Riyadh runway 01, taxied to a taxiway and then the crew told the tower that they would shut down the engines and evacuate. The engines were shut down but no evacuation was initiated so the fire and rescue personnel tried to open the doors. After 23 minutes (aircraft still pressurized) they managed to open R2 door. All 301 onboard were killed, the cause of the fire was never established.

Accident description (ASN).


December 23, 1980.

over Arabian Gulf.

Saudi Arabian Airlines, HZ-AHJ

L-1011-200 (serial no 1161).

An exploding tire blew a hole in the fuselage while in flight. Two passengers were sucked out of the aircraft in the rapid decompression that followed.

Accident description (AD).


May 4, 1983.

Miami-Nassau-Miami

Eastern Airlines, N334EA.

L-1011-1 (serial no 1141).

Flight 855 departed Miami for a 37 minutes trip to Nassau. When they descended through 15000 ft the low oil pressure light for the #2 engine illuminated. During the short flight all engines had indicated normal pressure and quantity but now the #2 engine showed low level (~8 qts) and pressure (~15-25 psi) while engines #1 and #3 still indicated normal. The #2 engine was shut down, the APU started, and with poor weather at Nassau the Captain decided to return to Miami. The flight was now down at 12000 ft and turned back towards Miami while climbing up to FL200.

When climbing through 15000 ft they got a low oil pressure light for the #3 engine. The Captain retarded the #3 throttle slightly and reduced the rate of climb. Then the #1 engine low oil pressure light illuminated. The gauges at the Flight Engineerīs panel showed that the oil pressure on both operating engines were low and falling and that all quantity gauges indicated zero. Since the risk of this happening is very slim the crew considered indication problems. They levelled off at 16000 ft at 300 kt and told ATC about their problems. ATC cleared them direct to Miami and speed was reduced to 230 kt.

Then, with no warning, the #3 engine failed. They were now flying on one engine. They radioed Miami and was cleared for a straight-in approach for runway 27L, still with 70 miles to go. They started a descend and also began dumping fuel. The weather at Miami was good and the crew now realized that the gauges were functioning properly. At 12000 ft also #1 engine failed. They were now 55 miles from Miami with no engines at all running. The rate of descend increased to 1600 ft/min with a speed of 225 kt and the crew now tried to restart engine #2 through windmilling. It did not start.

The cabin was prepared for ditching. The Captain would set it down on the water with the landing gear retracted, normal landing flaps and with the nose pitched up at 12 degrees. That would probably torn off the wing engines, flaps and horizontal stabiliser. The aircraft would still be expected to stay afloat for 20-25 minutes.

There was little hope of any successful restart of the wing engines but the crew tried it anyway, with no success. Now an airstarter assisted restart of engine #2 was carried out and at 4000 ft, still with 22 miles to Miami, it started. At 3000 ft they headed straight for runway 27L. On landing both engines #1 and #3 smoked badly bacause the fuel switches were still on from the previous start attempts and fuel was still beeing pumped. Fire bottles were discharged on both those engines.

The Captain asked for a tug to tow the aircraft away from the runway but was informed that there would be a delay for that. Then he tried to use the #2 engine only to find that there was no power available. The #2 engine failed on the runway.

The reason for all three engines losing all their oil was a magnetic chip detector replacement, on all engines, the previous night. The installed chip detectors were all missing their o-rings and when the engines were started they began to leak oil. A ten-second engine motoring was carried out at night to check for leaks but it was established later that a minimum of 30 seconds was required to get a leak with o-rings missing.

And about the start attempts on engine #2: The crew entered the chart incorrectly and tried a windmill start when an airstarter assisted one would be required. Later on, when they discovered that they needed airstarter assist the engine started. If they would have entered the chart correctly the first time - would the #2 engine have lasted all the way to Miami?

Read the full story in Stanley Stewartīs book "Emergency - Crisis on the Flight Deck".


August 02, 1985

Dallas, USA

Delta Airlines N726DA

L-1011-1 (serial no 1163).

DL191, from Fort Lauderdale, approached Dallas runway 17L in rain and thunderstorm. A microburst forced the aircraft down 6300 ft short of the runway. On impact it hit a car on a highway and struck two watertanks. It caught fire and of the 163 people onbord 134 were killed.

Accident description (ASN). Cockpit Voice Recorder transcript.

NTSB Animation download (1065kb).


May 3, 1986.

Colombo, Sri Lanka.

Air Lanka 4R-ULD

L-1011-100 (serial no 1061).

The flight from Colombo, Sri Lanka to Male, Maldives was delayed. During (the late) boarding a bomb, timed for an in-flight blast, exploded. Of the 128 people onboard, 14 were killed. The bomb, which destroyed the plane, was hidden in the aircraftīs "Fly-Away-Kit".

Accident description (ASN).


December 1989.

Cathay Pacific.

L-1011.

This incident involved a rear pressure bulkhead failure due to fatigue.

The below AAIB report contain lotīs of technical details of L-1011 pressure bulkhead problems, including some info about this incident.

AAIB report.


December 1990.

Air Canada.

L-1011.

This incident involved a rear pressure bulkhead failure.

The below AAIB report contain lotīs of technical details of L-1011 pressure bulkhead problems, including some info about this incident.

AAIB report.


Date unknown.

Pacific Ocean.

Delta Airlines.

L-1011.

Halfway between Los Angeles and Honolulu the Flight Engineer found the fuel quantity in one of the tanks to be decreasing at an abnormal rate. The crew decleared an emergency and started to crossfeed all engines from the leaking tank, to save fuel in the other tanks until it was needed.

The aircraft was prepared for what looked like a ditching and the Honolulu Coast Guard had been alerted for a possible intercept and resque operation. However, this was a lucky day, and they landed with very little fuel left onboard. The reason for the leak was a faulty fuel line.


June 28, 1991.

Dusseldorf, Germany.

LTU, D-AERI.

L-1011-1 (serial no 1114).

Aircraft destroyed by fire while undergoing maintenance (welding) in hangar. The ground crew managed to tow the aircraft out of the hangar, limiting the damages to only this aircraft.

Accident description (ASN).


July 30, 1992.

New York JFK, USA.

Trans World Airlines (TWA) N11002.

L-1011-1 (serial no 1014).

The aircraft took off from runway 13R at New Yorkīs JFK airport with 292 people onboard. When it became airborne, with the First Officer at the controls, the stickshaker was activated. The Captain took control of the aircraft and aborted the takeoff. Touchdown was made at 14 ft/sec (design limit 6 ft/sec) after 6 seconds in the air. Maximum brake and reverse was used and when the Captain understood that they could not stop before the runway end, he turned it to the left onto the grass. The airplane caught fire and was destroyed. The right Angle of Attack sensor had experienced 9 previous malfunctions, not detectable during cockpit preflight tests. The sensor gave a false warning when the airplane became airborne.

Accident description (ASN).


June 20, 1995.

Between Tenerife South and Faro.

Caledonian Airways, G-BBAH.

L-1011-100 (serial no 1101).

The aircraft departed Tenerife South for a flight to Manchester with 401 passengers onboard. I hour into the flight, at FL310, there was a loud "muffled bang" and a feeling of pressure in the ears. The Flight Engineers instrumentīs revealed that the cabin altimeter was climbing at approximately 2000 ft/min. The cockpit crew donned their oxygen masks and commenced an emergency descend. The Captain was now flying manually and the First Officer handled the radios. They were in contact with Casablanca Radio and radioed their emergency on that frequency.

In the cabin the crew also heard the bang (except for one attendant in lower galley) and felt pressure in their ears. The purser went to the Flight Engineer and told him that the oxygen masks were not deployed in the cabin. The F/E did that manually. The automatic system had not yet been activated because the cabin had not reached the preset altitude at that time. There was a smell of burning in the cabin because of the heat the oxygen generators produced.

The Captain levelled off at FL100 after a descent at a speed slightly less than the maximum operating speed. All system were found to be normal after the descend except for a "truck" light on the gear. The descend had been done with gear down.

At this time, the First Officer had established contact with Lisbon ATC. The aircraft position was approximately halfway between Tenerife and Faro so the Captain decided to divert to Faro. During the flight to Faro 4000 kg of fuel was dumped to bring the landing weight down to 160 000 kg.

The cabin was prepared for an emergency landing because of the landing gear "truck" light. As speed was reduced on final the "truck" light went out and the landing was normal.

The decompression was caused by a partial rupture (~300 x 400 mm) of the rear pressure bulkhead. The below AAIB report contain lotīs of technical details of this and other L-1011 pressure bulkhead problems.

AAIB report.


August 23, 1995.

Pacific Ocean.

Delta Airlines N781DL.

L-1011-1 (serial no 1003).

The aircraft was cruising at FL330 when a sudden decompression occured. The flight, with 236 people onboard, was at this time 450 miles west of the departure airport, Los Angeles. Destination was Honolulu. It landed safely even though the airframe was severly damaged. The aircraft is now used for ground tests by Lockheed.

Accident description (ASN).


October 31, 1996.

Gatwick, London, England.

Caledonian Airways, G-BBAH.

L-1011-100 (serial no 1101).

Engine #2 was started during pushback. After that, engine #3 was started but it failed to rotate so the start was abandoned. Engine #1 was then started with the intention to make another try at #3 after that. When #1 was started ATC reported smoke and flames from the tail of the aircraft. The crew had not observed that #2 TGT had increased and reached 250 degrees after 3 minutes.

The Airport Fire Service reacted very rapidly and sprayed the engine with foam. The crew were initially unaware of this action. Engineering assessed that the engine had suffered thermal shock from the foam and that corrosion damage had possibly occured to the adjacent aircraft structure. The fuel flow regulator was believed to be faulty.

AAIB report.


March 27. 1997.

New York, USA.

Delta Airlines N762DA.

L-1011-500 (serial no 1210).

The L-1011 was pushed back from the gate by a groundcrew of 3 employees. The tug operator was seated facing the airplane, while wing walkers were placed at the left and right wing tips. When the forward motion was initiated, the left and right wing walkers started to converge towards the tow bar, anticipating the disconnect of the airplane when it stopped. The left wing walker observed the right wing walker, the designated Dispatch Agent (DA) for the flight, approach the tow bar. The left wing walker glanced at the left wing tip, and when his vision returned to the tow bar, he saw the right wing walker under the nose wheel of the airplane. He was fatally injured.

NTSB report.


May 15, 1997.

Saint Louis, USA.

Trans World Airlines (TWA) N11003.

L-1011-1 (serial no 1015).

During climb passing FL290 the crew heard a loud bang. No abnormalities were found except for some vibrations near the left wing area. After landing at destination it was found that the left gear strut door had separated from the aircraft. Other damages from that failure was also detected.

NTSB report.


August 7, 1997.

Honolulu, Hawaii, USA.

Delta Airlines, N740DA.

L-1011-250 (serial no 1244).

After maintenance completed troubleshooting and the aircraft taxied out for the final time, the aircraft had taxied 11.3 miles within a 3-hour period. There was no temperature gauge or tabular data available that could have informed the crew that heat buildup resulting from taxi distance was now at a level that potentially threatened the integrity of the tires.

During the takeoff roll, the 3F tire exploded, resulting in vibration, shudder, and yaw. The sudden instability, combined with a phantom C1 cargo door light, caused the Captain to abort. The abort was initiated about Vr (165 knots) with approximately 6,000 feet of runway remaining. As the aircraft came to a stop, the nose wheels were 164 feet short of the overrun area for runway 8R. A brake fire began while the aircraft was stopping and the captain directed an emergency evacuation.

The 2R and 4R doors failed to open, and the 4L and 3L doors were not used due to their proximity to the fire and smoke. The 4R door was jammed by a broken piece of backboard, and the 2R door malfunctioned due to a partially broken counterbalance spring. The flight attendant who attempted to open the 2R door did not attempt to manually lift the door. All evacuations were made through the 1L, 1R, 2L, and 3R doors.

Firefighters had difficulty communicating with the flight crew and in verifying the total number onboard because the airline's passenger count does not include lap children. A total of 56 passengers and 2 flight attendants were treated for minor injuries, while 1 passenger received a broken ankle. All injuries were attributed to the use of the slides. Passengers failed to follow flight attendants and attempted to evacuate with their carryons. The airline did not effectively supervise the passengers after the evacuation and several began walking toward an active runway.

An inspection of the 3R tire showed bead separation had occurred. The estimated bead temperatures during the takeoff roll reached between 350 and 400 degrees Fahrenheit. The bead begins to degrade between 250 and 280 degrees Fahrenheit.

NTSB report.


October 20, 1997.

Gatwick, London, England.

Air Transat, C-FTNG.

L-1011-150 (serial no 1048).

When the aircraft started to accelerate at Gatwick runway 08R, "Hydraulic System" and "Flight Control Panels" warning lights illuminated on the "Warning and Caution Panel" (CAWP). "Rudder Hydraulic Limiter Push" illuminated on the overhead panel as well as "J Area Overheat" and hydraulic system A "Low Pressure Output" on the Flight Engineerīs panel. Hydraulic system A quantity gauge also indicated loss of fluid. The Captain aborted the takeoff and at the same time the tower radioed that smoke was coming from one of the engines.

The aircraft slowed down on the runway, max speed had only been 68 kt, and taxied off and stopped on a high-speed exit. Fire and resque crew saw that smoke was coming from the leading edge of the tailplane and from a grill at the bottom of the fuselage. Cabin crew also reported light smoke entering the cabin in the rear.

A controlled evacuation was initiated using the two front slides on each side of the aircraft. It took 10 minutes to evacuate 357 passengers and 11 suffered minor injuries.

Examination showed that an elbow section of a large bore titanium duct, delivering air from No 2 engine bleed system, had blown out. This had caused secondary damage to adjacent hydraulic pipes in 'A' and 'B' systems which accounted for the observed hydraulic system failures. Further examination showed that the failure had been caused by a massive over pressurisation of the air duct.

AAIB report.


February 06, 1998.

Panama City, Panama.

American Int`l Airways, N103CK.

L-1011-200F (serial no 1212).

---This is preliminary information, subject to change, and may contain errors.---

American International Airways (Connie Kalitta Services) flight 840, experienced blown tires during an aborted takeoff from the Tocumen International Airport, Panama City, Panama. Visual meteorological conditions prevailed at the time and an IFR flight plan was filed for the nonscheduled, international, cargo flight. The airplane was not damaged and the airline transport-rated captain, first officer, flight engineer, and two additional crewmembers were not injured.

The flight was originating at the time of the incident. According to officials from the Government of Panama, the captain elected to use a runway that was 2,000 feet shorter than the longer of the parallel runways. During the takeoff after the nose landing gear was rotated the captain elected to abort. After touchdown all main landing gear tires were blown and the airplane was stopped on the runway.

NTSB preliminary report.


May 31, 1998.

Manchester, England.

EI-COL.

L-1011-1 (serial no 1036).

The aircraft was flown manually for a landing at Manchester runway 24R. Landing data card showed a landing weight at 304 000 lb with a VREF at 129 kt. The pilot handling the aircraft felt that the rate of descend did not reduce as normal during the flare so he increased the pitch attitude which resulted in a tail strike. After touchdown the Flight Engineer commented that the pitch attitude at touchdown was about 15 degrees. Only minor damage occured to a drain mast, antenna, tail bumper and a small skin area.

The DFDR was malfunctioning and contained no data. A final approach profile could still be constructed using height calls from the CVR and recorded radar data. That profile showed that the rate of descend increased below 100 ft AGL and that the flare appeared to be ineffective.

Company procedures was that the Captain prepared the loadsheet, in lbs, and the Flight Engineer calculated Take Off and Landing Data Cards. At the departure station all figures were given in kilos. They were converted to lbs except for passenger weight which was still in the kilo figure on the loadsheet. This meant that the aircraft was 22 000 lbs heavier than the loadsheet figure. The correct VREF for the landing should have been 136 kt.

On the previous sector the loadsheet contained exactly the same mistake but that approach was flown by the other pilot at a slightly higher speed with a normal landing.

AAIB report.


December 22, 1998.

Atlanta, Georgia.

Delta Airlines, N766DA

L-1011-500 (serial no 1207).

---This is preliminary information, subject to change, and may contain errors.---

Just before pushback from the gate, a passenger seated immediately aft of L2 door, saw sparks and smoke from a vent below the sidewall panel. The Captain was notified and everyone left the aircraft through the forward exit. The flight was cancelled.

Maintenace personnel was called for and down in the MESC, they found two wire bundles, about 3 inches in diameter, that were burnt. The wire bundles were coloured blue from leaking toilet fluid. The wire bundles were repaired and the aircraft was back in service after 6 days.

The mid toilets on Delta aircraft have a "low charge level" and therefor have an increased risk of beeing overfilled. In that case the excessive fluid may end up on electrical wiring.

Delta Airlines now has a "Special Inspection" of the wires, the toilet drip pan and the drain tubes in the MESC. There has been a great number of reports of fluid, dirt, dust and metal debris in the inspection area.

NTSB preliminary report.


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